New Build Steel Frame Router
Posted: Mon May 06, 2024 8:40 pm
Ok, Finally posting here my CNC Router. Its aprox 2' x 4' steel frame moving gantry. I built it with a pretty limited tools, welder, grinder, jig saw and drill press. I used self leveling epoxy to create flat surfaces for the linear rails. I am using stepperonline closed loop steppers Nema 34 CL86T. When I first commissioned the machine, I purchased a small linear stage for the Z axis. I had some wooden parts to get things working. Eventually I used the router to build parts for an alloy Z axis. I recently upgraded the ball screws from 1605 to 2010. The original screws were bent, and would whip at speeds over about 100ipm. Also they had about 0.002" backlash. I can get 500 ipm with the new ballscrew, they are very straight, and less than 0.0005" backlash.
The machine is a hobby for me. I design custom surf hydrofoils. I machine female molds out of MDF. I use the molds to laminate carbon fiber in a top and bottom half to make the hydrofoils. I run a parallel tool path with very fine 0.010 stepover. Some cycles run 4-6 hours. Never had any issues. I use precision mill as the smoothing setup. The results are superb, almost no sanding required, corners are sharp and crisp as they should be. I learned a lot and had fun building the machine. I am very happy with the Centroid Acorn board and CNC12 software. As long as you follow the instructions, everything just works.
I am always learning new things and trying to improve accuracy. I am trying to figure out how to improve the roundness of a bore tool path. Currently I get an oblong hole. With a climb cut the long part of the hole is at +45 deg to the +X axis with Conventional the long axis is at +135 deg. Hard to measure accurately MDF with calipers, but The longest part of the bore is about +.005" to +.010" for a 0.750" bore. The slower feeds produce more round holes. Speeds are 75 ipm to 35 ipm. I am running a spring pass. I was expecting a large improvement by replacing the ballscrews with considerably less backlash, and a much more rigid Z Axis. What am I missing?
The machine is a hobby for me. I design custom surf hydrofoils. I machine female molds out of MDF. I use the molds to laminate carbon fiber in a top and bottom half to make the hydrofoils. I run a parallel tool path with very fine 0.010 stepover. Some cycles run 4-6 hours. Never had any issues. I use precision mill as the smoothing setup. The results are superb, almost no sanding required, corners are sharp and crisp as they should be. I learned a lot and had fun building the machine. I am very happy with the Centroid Acorn board and CNC12 software. As long as you follow the instructions, everything just works.
I am always learning new things and trying to improve accuracy. I am trying to figure out how to improve the roundness of a bore tool path. Currently I get an oblong hole. With a climb cut the long part of the hole is at +45 deg to the +X axis with Conventional the long axis is at +135 deg. Hard to measure accurately MDF with calipers, but The longest part of the bore is about +.005" to +.010" for a 0.750" bore. The slower feeds produce more round holes. Speeds are 75 ipm to 35 ipm. I am running a spring pass. I was expecting a large improvement by replacing the ballscrews with considerably less backlash, and a much more rigid Z Axis. What am I missing?