I got pretty busy with work so I haven't had as much time to work on my conversion but I did manage to get a couple of things done.
I used to constantly stand around with a vacuum hose in one hand trying to vacuum up chips and apply cutting fluid at the same time while running the machine. I got really tired of fumbling around with cans of wd-40, oil cans, acid brushes, spray bottles, and making a mess everywhere..... I was also getting real tired of vacuuming up chips all over the garage and the machine.
A few years back I came across some 1/2 polycarbonate sheet that was being scrapped because it had some scratches and decided to make a chip shield for my bridgeport with it. I made it fit the entire work envelope of the machine. There is an aluminum channel I welded up that the front panel slides in and out of. There is a permanent piece on the front bottom that the vise socket fits through. I plan on drilling more holes in the front bottom piece as I move the vise around the table.
I Made the back out of 1/4" flexible expanded pvc as it is possible to crash this piece if the Y axis is jogged too far forward with the knee cranked up high. This position would be very rare on my machine but the possibility exists and I want to be safe. I also welded up an aluminum channel so I can fit a different height piece in case the knee has to be cranked up really high to give some clearance and have some chip shielding.
I also decided to make my own fog-less coolant sprayer. They are real simple to build. There are plans floating around the net to build these.
Automation Direct has a nice 24vdc 3port 2 way air solenoid that works very well with the acorn for automatic mist cooling. No more fumbling around with spray cans and acid brushes. What's really nice is the mister uses so little fluid that the chips are almost dry and are easy to clean up out of the chip shield. I need to install a check valve inline the coolant hose because if I don't use it for a couple of days, gravity drains the coolant back into the canister. Not a big issue as all I have to do is open the needle valve and purge the line. I'm figuring a check valve will fix this small issue.
Please mind the messy wiring....