I saw his post, I didnt know that he was trying to tell me that my z and x was swapped. Hmm... I set my lathe up like in the attached picture. Is this wrong?brittfussel wrote: ↑Fri Oct 25, 2019 8:44 pm October 25, 2019
Kevin
Will do on Monday when I'm back in the shop.
Did you look at Marty's post above? Your report is suggesting that you have your x and z-axis swapped?
Britt
shoptask turnado lathe to acorn
Moderator: cnckeith
-
- Posts: 36
- Joined: Mon Apr 22, 2019 10:33 pm
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: No
- Oak CNC controller: No
- CNC Control System Serial Number: none
- DC3IOB: No
- CNC12: Yes
- CNC11: No
- CPU10 or CPU7: No
Re: shoptask turnado lathe to acorn
Shoptask turnado lathe converted to acorn (when I finally receive the machine)
Plasma table build with acron
Plasma table build with acron
(Note: Liking will "up vote" a post in the search results helping others find good information faster)
-
- Community Expert
- Posts: 3524
- Joined: Tue Mar 22, 2016 10:03 am
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: Yes
- Oak CNC controller: Yes
- CNC Control System Serial Number: 100505
100327
102696
103432
7804732B977B-0624192192 - DC3IOB: No
- CNC12: Yes
- CNC11: No
- CPU10 or CPU7: No
- Location: Boston, MA
- Contact:
Re: shoptask turnado lathe to acorn
That's how I have my lathes set up.
Cheers,
Tom
Confidence is the feeling you have before you fully understand the situation.
I have CDO. It's like OCD, but the letters are where they should be.
Tom
Confidence is the feeling you have before you fully understand the situation.
I have CDO. It's like OCD, but the letters are where they should be.
(Note: Liking will "up vote" a post in the search results helping others find good information faster)
-
- Community Expert
- Posts: 9944
- Joined: Tue Mar 28, 2017 12:01 pm
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: Yes
- Oak CNC controller: No
- CNC Control System Serial Number: none
- DC3IOB: No
- CNC12: Yes
- CNC11: Yes
- CPU10 or CPU7: Yes
- Location: Mesa, AZ
Re: shoptask turnado lathe to acorn
Your picture is correct. I am questioning the accuracy of your turns per inch on X and Z
Reminder, for support please follow this post: viewtopic.php?f=20&t=383
We can't "SEE" what you see...
Mesa, AZ
We can't "SEE" what you see...
Mesa, AZ
(Note: Liking will "up vote" a post in the search results helping others find good information faster)
-
- Posts: 36
- Joined: Mon Apr 22, 2019 10:33 pm
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: No
- Oak CNC controller: No
- CNC Control System Serial Number: none
- DC3IOB: No
- CNC12: Yes
- CNC11: No
- CPU10 or CPU7: No
Re: shoptask turnado lathe to acorn
Ok so after all the posts I recieved tonight, I went out to the shop to check some things.
My z axis is indeed belt drive with 2 gears, and it does in fact seem to be 1:1 ratio My x axis is direct drive with coupler So I think Marty is correct with the diameter mode and why my x axis revs per inch are double. To clarify, when I do a g0 x1 command, that should move the x axis .5" and not 1" correct?
Would this also explain why my x axis seems to move twice as fast as my z axis even though the speeds are the same in the wizard?
My z axis is indeed belt drive with 2 gears, and it does in fact seem to be 1:1 ratio My x axis is direct drive with coupler So I think Marty is correct with the diameter mode and why my x axis revs per inch are double. To clarify, when I do a g0 x1 command, that should move the x axis .5" and not 1" correct?
Would this also explain why my x axis seems to move twice as fast as my z axis even though the speeds are the same in the wizard?
Shoptask turnado lathe converted to acorn (when I finally receive the machine)
Plasma table build with acron
Plasma table build with acron
(Note: Liking will "up vote" a post in the search results helping others find good information faster)
-
- Community Expert
- Posts: 9944
- Joined: Tue Mar 28, 2017 12:01 pm
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: Yes
- Oak CNC controller: No
- CNC Control System Serial Number: none
- DC3IOB: No
- CNC12: Yes
- CNC11: Yes
- CPU10 or CPU7: Yes
- Location: Mesa, AZ
Re: shoptask turnado lathe to acorn
I think you have your turns ratio wrong on X. Test it like I said. Turn the screw, count how many turns it takes to move the axis 1". Enter that value for X to start with.KevinTaylor wrote: ↑Fri Oct 25, 2019 10:43 pm Ok so after all the posts I recieved tonight, I went out to the shop to check some things.
My z axis is indeed belt drive with 2 gears, and it does in fact seem to be 1:1 ratio
zaxis-beltdrive.jpg
My x axis is direct drive with coupler
coupler.jpg
So I think Marty is correct with the diameter mode and why my x axis revs per inch are double. To clarify, when I do a g0 x1 command, that should move the x axis .5" and not 1" correct?
Would this also explain why my x axis seems to move twice as fast as my z axis even though the speeds are the same in the wizard?
Yes. Tell the control you want to remove 1" of material, X only moves .5". Lathe defaults to diameter mode.
Reminder, for support please follow this post: viewtopic.php?f=20&t=383
We can't "SEE" what you see...
Mesa, AZ
We can't "SEE" what you see...
Mesa, AZ
(Note: Liking will "up vote" a post in the search results helping others find good information faster)
-
- Posts: 44
- Joined: Fri Oct 19, 2018 5:47 pm
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: No
- Oak CNC controller: No
- CNC Control System Serial Number: none
- DC3IOB: No
- CNC11: No
- CPU10 or CPU7: No
Re: shoptask turnado lathe to acorn
October 25, 2019
Kevin
I made the assumption that your z-axis was the same as mine: belted with a 2:1 ratio. I see that your machine is 1:1 on the z-axis. I've been pondering that modification to mine.
If you calibrated your x-axis in diameter mode, and if you were expecting the table to move one inch when you commanded it to move one inch, your turns per inch would result in a number 10.16 plus. Change it to radius mode and command it to move one inch. It should move two inches. I don't think this is your problem though. I believe you should still test it with something of a known dimension such as a gage block or 1-2-3 block.
Britt
Kevin
I made the assumption that your z-axis was the same as mine: belted with a 2:1 ratio. I see that your machine is 1:1 on the z-axis. I've been pondering that modification to mine.
If you calibrated your x-axis in diameter mode, and if you were expecting the table to move one inch when you commanded it to move one inch, your turns per inch would result in a number 10.16 plus. Change it to radius mode and command it to move one inch. It should move two inches. I don't think this is your problem though. I believe you should still test it with something of a known dimension such as a gage block or 1-2-3 block.
Britt
(Note: Liking will "up vote" a post in the search results helping others find good information faster)
-
- Community Expert
- Posts: 9944
- Joined: Tue Mar 28, 2017 12:01 pm
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: Yes
- Oak CNC controller: No
- CNC Control System Serial Number: none
- DC3IOB: No
- CNC12: Yes
- CNC11: Yes
- CPU10 or CPU7: Yes
- Location: Mesa, AZ
Re: shoptask turnado lathe to acorn
Here is what I do.
I put a dial indicator, on the slide of the X axis, parallel with the X axis. I put a right angle plate down perpendicular to the X axis. I jack it up on 1-2-3 blocks if needed. I move the indicator to the angle plate to take up backlash, I jog the indicator tip into the angle plate until it reads 0.
I set a part zero on X.
I go into MDI.
I do a G98 so I can move without the spindle turning (my machines have encoders)
I command a G01X-1.0F5 move. I watch and count the rotations of the indicator and see where it lands.
Let's say it moved .499"
BUT I commanded a 1" move, which is actually .5" (diameter mode)
So I take .5" and divide it by the actual moved distance of .499", which equals 1.00200401. I then go into the Wizard and then multiply that number by the turns ratio currently in the Wizard, enter the new value in the Wizard and retest.
For Z, I chuck my 2" indicator (gently in the jaws), and set the angle plate ON the X cross slide perpendicular to the axis. I jog the cross slide in the Z- direction to take up backlash and zero my indicator, set my Z part Zero, command a G01 Z-1.0 F5. This time I use the commanded distance to travel, 1" and divide it by the actual distance travelled, then multiply it by the turns ratio in the Wizard, replace the number in the turns ratio with the new value.
When I am done calibrating the axis. I repeat, the above, but this time I command a move back to the original 0 position, the difference between 0 and where it landed is my backlash. I enter that into the backlash table. Retest. That usually takes care of everything. Probably other ways to do a lathe, but that's how I do it.
I hope that makes some sense. I just finished setting up 3 benchtop lathes for a customer that way.
Marty
I put a dial indicator, on the slide of the X axis, parallel with the X axis. I put a right angle plate down perpendicular to the X axis. I jack it up on 1-2-3 blocks if needed. I move the indicator to the angle plate to take up backlash, I jog the indicator tip into the angle plate until it reads 0.
I set a part zero on X.
I go into MDI.
I do a G98 so I can move without the spindle turning (my machines have encoders)
I command a G01X-1.0F5 move. I watch and count the rotations of the indicator and see where it lands.
Let's say it moved .499"
BUT I commanded a 1" move, which is actually .5" (diameter mode)
So I take .5" and divide it by the actual moved distance of .499", which equals 1.00200401. I then go into the Wizard and then multiply that number by the turns ratio currently in the Wizard, enter the new value in the Wizard and retest.
For Z, I chuck my 2" indicator (gently in the jaws), and set the angle plate ON the X cross slide perpendicular to the axis. I jog the cross slide in the Z- direction to take up backlash and zero my indicator, set my Z part Zero, command a G01 Z-1.0 F5. This time I use the commanded distance to travel, 1" and divide it by the actual distance travelled, then multiply it by the turns ratio in the Wizard, replace the number in the turns ratio with the new value.
When I am done calibrating the axis. I repeat, the above, but this time I command a move back to the original 0 position, the difference between 0 and where it landed is my backlash. I enter that into the backlash table. Retest. That usually takes care of everything. Probably other ways to do a lathe, but that's how I do it.
I hope that makes some sense. I just finished setting up 3 benchtop lathes for a customer that way.
Marty
Reminder, for support please follow this post: viewtopic.php?f=20&t=383
We can't "SEE" what you see...
Mesa, AZ
We can't "SEE" what you see...
Mesa, AZ
(Note: Liking will "up vote" a post in the search results helping others find good information faster)
-
- Posts: 36
- Joined: Mon Apr 22, 2019 10:33 pm
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: No
- Oak CNC controller: No
- CNC Control System Serial Number: none
- DC3IOB: No
- CNC12: Yes
- CNC11: No
- CPU10 or CPU7: No
Re: shoptask turnado lathe to acorn
I reset my x axis revs per inch and it is correct now. The new number for my x axis is 5.110149884.
I also checked my machines DRO against the 2" plunger DTI and they seem to be fairly accurate with each other.
My machines DRO says 2.009 My DTI says the same thing So while I haven't completely ruled out that my machines DRO is off, it seems its not my problem with my x axis.
The further I go in x+ the more off it becomes. At just 2" it is already off by 9thou. And that number keeps increasing the further out I go in x+.
Again just to make sure in case what I have done is already buried in my thread, I have adjusted the x axis gib. I have tightened the x axis thrust bearing. I have taken out the ball screw and ball screw mount -> reinstalled and made sure all bolts are tight. I have upgraded my limit switches to metrol (which are supposed to be good I hear), and I have replaced the direct drive coupling.
Could it be a bad stepper motor? I have no clue as how to proceed at this point. Any suggestions?
I also checked my machines DRO against the 2" plunger DTI and they seem to be fairly accurate with each other.
My machines DRO says 2.009 My DTI says the same thing So while I haven't completely ruled out that my machines DRO is off, it seems its not my problem with my x axis.
The further I go in x+ the more off it becomes. At just 2" it is already off by 9thou. And that number keeps increasing the further out I go in x+.
Again just to make sure in case what I have done is already buried in my thread, I have adjusted the x axis gib. I have tightened the x axis thrust bearing. I have taken out the ball screw and ball screw mount -> reinstalled and made sure all bolts are tight. I have upgraded my limit switches to metrol (which are supposed to be good I hear), and I have replaced the direct drive coupling.
Could it be a bad stepper motor? I have no clue as how to proceed at this point. Any suggestions?
Shoptask turnado lathe converted to acorn (when I finally receive the machine)
Plasma table build with acron
Plasma table build with acron
(Note: Liking will "up vote" a post in the search results helping others find good information faster)
-
- Community Expert
- Posts: 9944
- Joined: Tue Mar 28, 2017 12:01 pm
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: Yes
- Oak CNC controller: No
- CNC Control System Serial Number: none
- DC3IOB: No
- CNC12: Yes
- CNC11: Yes
- CPU10 or CPU7: Yes
- Location: Mesa, AZ
Re: shoptask turnado lathe to acorn
Did you supply the stepper motors or were they on the machine?
What drives are being used?
What voltage power supply is being used?
Sorry, I can't spend the time to wade through 6 pages of posts.
Are you GAINING or LOSING?
X+ is AWAY from the spindle center line. That how you have the machine setup correct?
Carriage AWAY from the headstock is Z+
What drives are being used?
What voltage power supply is being used?
Sorry, I can't spend the time to wade through 6 pages of posts.
Are you GAINING or LOSING?
X+ is AWAY from the spindle center line. That how you have the machine setup correct?
Carriage AWAY from the headstock is Z+
Reminder, for support please follow this post: viewtopic.php?f=20&t=383
We can't "SEE" what you see...
Mesa, AZ
We can't "SEE" what you see...
Mesa, AZ
(Note: Liking will "up vote" a post in the search results helping others find good information faster)
-
- Posts: 36
- Joined: Mon Apr 22, 2019 10:33 pm
- Acorn CNC Controller: Yes
- Allin1DC CNC Controller: No
- Oak CNC controller: No
- CNC Control System Serial Number: none
- DC3IOB: No
- CNC12: Yes
- CNC11: No
- CPU10 or CPU7: No
Re: shoptask turnado lathe to acorn
The stepper motors were supplied with the machine.martyscncgarage wrote: ↑Sat Oct 26, 2019 5:17 pm Did you supply the stepper motors or were they on the machine?
What drives are being used?
What voltage power supply is being used?
Sorry, I can't spend the time to wade through 6 pages of posts.
Are you GAINING or LOSING?
X+ is AWAY from the spindle center line. That how you have the machine setup correct?
Carriage AWAY from the headstock is Z+
It is using a gecko g540.
48v power supply I believe.
I am gaining.
My machine is set up exactly like in the attached picture.
Shoptask turnado lathe converted to acorn (when I finally receive the machine)
Plasma table build with acron
Plasma table build with acron
(Note: Liking will "up vote" a post in the search results helping others find good information faster)